John S's Journal
Home Page: John S
Eugene, OR, USA
| Total Posts: 182 | Latest Post: 2026-03-25 |
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I took highway 99W which is a nice 2 lane road through some small towns in the Willamette Valley. Beautiful day and light traffic so it was a treat to get the GT out beyond the comforts of the local roads that I have been driving as I dialed in the tuning of the car after receiving the original 25D back from Jeff and the rebuilt HS4’s from Joe. Having a chance to experience the OD on a long trip was something that I was looking forward to and it made a huge difference in comfort being able to cruise at lower rpm’s.
A 160 mile round trip with zero issues really boosted my confidence in the reliability of my car so I’m looking forward to just being able to jump in it and go now. Took it to have the front end alignment checked and adjusted this morning and my guesswork after the front suspension rebuild was fairly close. Nice to have it dialed in although it tracked and handled pretty well on the trip.
The list of things to do has narrowed down to finishing the front valance which stalled out after the carbs showed up. It’s in epoxy primer just awaiting some time and motivation to skim with some filler, sand and paint. Then the bumper can go back on. A couple guys at the show said to leave it off to show off the nice, powder coated suspension but it looks unfinished to me so I’ll get to it eventually.
Although it worked when I bench tested it months ago, I always wondered if I did a good job servicing the Craigslist gearbox that I purchased on the cheap. I hadn’t intended on doing anything other than replacing the easy to get to o-rings, seals, gaskets, etc. but that changed when the pump assembly dropped down into the abyss. As long as I had to take the OD unit off, I replaced the o-rings on the pistons as well. Today’s drive reassured me that I didn’t bungle anything up when I reassembled it.
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I’ve got some heavy granite tiles leftover from a project so I glued a sheet of 320 grit wet/dry paper to it and got every flange surface smooth and flat after removing the studs.Maybe a half hours worth of sanding. Removed all of the HS4 hardware from the GT, put some #2 Permatex on all of the gasket surfaces and buttoned everything back up. Went through the whole procedure, synched the carbs, mixture, idle, etc. , rechecked the timing and backed it off a bit, quick test drive and was pleasantly surprised at how it performed. I still feel as though I really had to lower the jets quite a bit but didn’t pull the dash pots. Didn’t have much gas in the tank and not much time either so there is more testing to do and analyzing plugs, and probably pull the dash pots to see where I wind up. Maybe the old girl just needs the jets lower than most of the other cars Inread about. Time will tell.
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